

![]() posts: 1637 Essex group joined on Mon 17th Nov 2008 |
RBRR 2016. Another Success! |
|
|||
---|---|---|---|---|---|
Friday the 7th October 2016 and the long awaited Club Triumph Round Britain Reliability Run was upon us. Hopes of a nice lay in were soon dashed when the neighbour across the road was having his driveway block paved and I was awoken by the sound of a nine inch angle grinder revving its nuts off! Moving into the lounge wasn't much better as the house behind me was also doing some building work with the aid of a kango! How's your luck? My two co-drivers (Darren Sharp and Dave Saunders) arrived just before 2pm and after a quick coffee we were ready to set out. However, Dave then noticed a spring laying in the driver side footwell. Further investigation revealed that the clutch return spring had broken and just dropped off of the pedal! Dave and Darren then proceeded to remove the parcel tray while I disappeared into the Garage to rob the spring from my Mk1 Pi. (See? It pays to have more then one car!) Once this awkward and fiddly job was done, we were finally ready to set off, although now an hour later than we intended. The traffic around the M25 and A1 wasn't too bad and before long we were at the start location at Knebworth. I always love the start of this event and meeting other club members that you wouldn't normally see is always a highlight for me. Before long we were setting out, and leaving Knebworth turned out to be a lot better than leaving the previous location for the RBRR. No traffic hold ups at all. Lovely! A quiet drive up the A1 saw us arrive at the first check point at Blyth more or less at the opening time. A quick stop for fuel and signing of the roadbook and we were away again. We had to devise a diversion for the next bit as the A1 was closed at Leeming Bar for bridge works. We opted to take the A168 and A19 and then cut back over not far short of the next control at Carter Bar. (The Scottish Border) Arrival at Carter Bar 20 mins early found the check point initially void of any CT marshal's, but by the the time it was due to be open, they had arrived. A quick dash up to Kinross Services for the next control saw us take on fuel again and then it was my turn for the long run up past Inverness and the next control at Skiach services. After more coffee at Skiach to boost the energy levels we then encountered the beautiful drive up to John O Groats while watching the sun rise over the North Sea.
With Gertie full of 99 octane and us full of coffee and hot fried food we left Seaview earlier than intended, but only to vacate the table for more incoming crews. A leisurely drive was then taken across the top of Scotland through Thurso and over to Bettyhill before heading south towards Altanharra. The next control point was back at Skiach and because we left JOG so early we were there a good hour before it opened. This was fine with us as Dave wanted to grab more sleep and Darren and I did some fine tuning with the car. I then took my seat behind the wheel for (in my opinion) the best part of the run. We went down past Loch Ness and Fort William and stopped at a lovely roadside cafe just before Glencoe for a nice piece of Lemon Drizzle cake and more coffee. Darren was now in the driving seat and I tried to grab some sleep on the back seat as for some reason, sleep had totally evaded me so far. The Gledrid control was its usual hive of activity and it's at this point that I took to consuming Red Bull and Haribo TangFastics sweets in readiness for the pitch black Welsh forest stages down to Sugar Loaf. The Sugar Loaf control was crammed so we just pulled in, had the book signed and moved on. Another good drive saw us topping up with fuel at the previous control at Gordano, before carrying on down to Westonzoyland aerodrome and the next control. Coffee and Banana cake was the order of the day here before the long slog down to Lands End via the check point at Okehampton. Sunday morning saw us at Lands End and finally in the daylight again. This is the part of the run where we all start perking up. The daylight driving makes life easier, plus you know that you are on the last leg and homeward bound. (Well heading for the finish anyway) Another good hearty breakfast saw us revitalised and heading for Bude Motor Museum. More coffee followed and I made arrangements to leave my timing light and spare distributor for my fellow CT Essex colleagues in car 104 who were having a few difficulties and were about 90 mins behind us. From Bude we headed for Badger Holt at Dartmoor where we enjoyed ice cream purchased from the petrol money. (Such Luxuries!) Pimperne would be the next control and famous (with CT anyway) for the vast array of cakes laid on. This is always a favourite haunt for RBRR'ers and nobody ever seems to be in a rush to get away from here. This was the penultimate control, so the drive from here is always full of apprehension and the dread of something going wrong at this late stage. The rain also set it at this point which was a pity as this had been the best RBRR for weather since my first one in 2010. The drive back to the finish was the usual Sunday night go slow, but not too bad actually. We made Knebworth in good time and walking up to the bar I was met by a giant dog serving beer! I thought I must have been more tired than I thought and had starting hallucinating, but it turned out to be one of the bar staff in a dog costume. =) We had booked into the hotel for the night, so no more driving for us and we had the chance to have a few beers to round off a great weekend. We'd had another great run and once again Gertie had performed faultlessly. (Apart from the broken clutch spring at the start) This was now her 3rd RBRR in my ownership and 4th in total. All without breakdown or serious issue. I have to say though, I may stand her down for the next one and give the Mk1 Pi a try. Listening to all those other Pi's on the run just made me want to be in the same.posted Sun 16th Oct 2016 |
![]() posts: 1637 Essex group joined on Mon 17th Nov 2008 |
RBRR - 1 month to go......Gearbox out again!!! |
|
|||
---|---|---|---|---|---|
Since about May this year I have had a strange tinny rattling sound on Gertie. However, this sound only happens when you turn the engine off. You never hear it when driving along. The noise is very similar to having a loose exhaust clamp which is spinning round the exhaust. So, that was where the investigations started. Over the past few months extensive investigations have also been carried out on the starter motor, alternator and various other parts that rotate. I've also laid underneath the car while someone starts it and turns it off again looking for this noise, I've looked through the engine bay, up inside the nose cone in case the electric fan brackets had come loose or broken, you name it, I've looked there. I eventually convinced myself that it was coming from the bellhousing area, so when after all else had failed, I resigned my self to removing the gearbox. (Not my favourite job- I think this is the 4th time since 2011 now!) Inspection of the gearbox proved to be fine and everything looks and works as it should. However, I then tried to push my finger through the splined hole for the clutch plate and felt something very loose and flapping about. Removal of the clutch plate revealed the below. I'm not too impressed I have to say. Particularly as this clutch was only 14 months old when it started making this noise. You can see the crack in the bottom left of the hexagonal metal plate. This metal plate was obviously dropping onto the first motion shaft and spinning round it when the engine was switched off. Maybe it was doing while driving along as well, but I couldn't hear it because of the engine noise. Or, maybe the centrifugal force of the flywheel was moving it back into place while circulating? Who know? All I know is, I need another bloody clutch! =(
posted Sun 4th Sep 2016
|
![]() posts: 1637 Essex group joined on Mon 17th Nov 2008 |
RBRR Preparations. |
|
|||
---|---|---|---|---|---|
On the last part of the recent Scottish trip Dave and I had become aware that the brake pedal had a tad more travel than normal. Once home and time permitted inspections revealed that the front pads were indeed getting low. Replacements were purchased and while I was at it I decided to replace the rear shoes as well. Further inspections revealed that the nearside inner front wheel bearing was noisy, so I replaced all of the front wheel bearings. My train of thought being that they were all fitted at the same time, so if one was worn, the rest may not be that far behind. Plus, I'd rather do the job now in a nice warm garage with plenty of light and tools, rather than on the RBRR in a pitch black lay-by somewhere while it's peeing down with rain and watching my sockets roll down a drain hole! (Or worse still the replacement bearing!) With this done I then focused on the shock absorbers. Gertie has become a bit 'wallowy' of late and needed to be tightened up a bit. A full set of brand new gas shocks were purchased and fitting commenced. The rears had been replaced with new standard shocks a few years back so these were swapped with the new gas items and put in the spares bin. The front shocks however, had never been replaced.In fact, if I remember rightly I had swapped the entire front legs over off of my Mk2 before I sold it so that I could keep my lowered springs. Once I had stripped the legs right down and removed the shocks I discovered that the driver side had a Monroe gas shock in it, but the passenger side had a normal hydraulic one! I can't believe that people can do these things. Both gaiters were completely knackered as well, so a new pair were ordered. The new shocks were fitted, then the search began for a replacement strut top as my nearside one had seized solid and this had caused the rubber bonding to split. You wouldn't have thought so though as the car steered perfectly. It's amazing what power steering can mask! So with this little lot done, all that's needed before the RBRR is an oil and filter change, then we are all good to go and Gertie will have another sticker for the inside of her bootlid. :) I've been doing bits to the Pi as well. I finally got fed up of the 'super lightweight', vague and constantly leaky steering and removed all of the power steering kit. I also re-greased the strut tops while I was at it and set the Koni Adjustable front shocks for a bit more 'firmness'. The Pi steering wheel has also been removed for something with more strength in the form of a Motolita. (No, the Pi wheel isn't for sale) :) The next job was to remove the awful Mk2 rear brakes that someone had fitted. The so called 'self adjusting' handbrake type that do nothing of the sort! Mk1 back plates were sourced, new wheel cylinders and brake shoes were fitted and now at last I have a car that I can park on a hill and it will still be there when I get back. An oil and filter change is also next on the list for this car too. Plus, I've almost got a full set of good doors and panels for her now, so the bodywork should start taking shape soon as well. I just really need to get out and drive the bloody thing more. It goes like stink when required and sounds fantastic too. |
Club Triumph Ltd. Registered in England No. 4961210 Registered Office: Suite A,10th Floor, Maple House, High Street, Potters Bar, Herts, EN6 5BS. VAT registration number 340 4536 26. Club Triumph is run entirely by its members for its members and does not have paid employees.
Website Terms and Conditions | Terms and Conditions of Sale | Privacy |Club Rules